Design 2: Wood Bot Maneuverability Testing
Posted by hkhalid2 on April 12, 2019
Filed under Uncategorized
Date: March 30, 2019
On March 30th, testing of body design 2 was complete. Since there was no changes in wiring or components from body design 1, coding and components were carry over to second body design. After transition from PVC pipes to wood, we conclude that the body design 2 is more stable and sturdy in test trial although the motors and wheels were securely attach, the turning mechanic does not function properly due to a lack of power supply from the motors. In ordering to resolve this issue, we decided to implement a gear ratio design to increase power to wheels. Team member Dean was in charge of designing the 3D-printed model of the gears and how to implement it in the wheel design.
Comments
Leave a Reply