Design 2: Wood Bot Maneuverability Testing

Posted by on April 12, 2019 
Filed under Uncategorized

Date: March 30, 2019

On March 30th, testing of body design 2 was complete. Since there was no changes in wiring or components from body design 1, coding and components were carry over to second body design. After transition from PVC pipes to wood, we conclude that the body design 2 is more stable and sturdy in test trial although the motors and wheels were securely attach, the turning mechanic does not function properly due to a lack of power supply from the motors. In ordering to resolve this issue, we decided to implement a gear ratio design to increase power to wheels. Team member Dean was in charge of designing the 3D-printed model of the gears and how to implement it in the wheel design.

 

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